četvrtak, 31. ožujka 2011.

Chernobyl disaster



The Chernobyl disaster was a nuclear accident that occurred on 26 April 1986 at the Chernobyl Nuclear Power Plant in the Ukrainian SSR (now Ukraine). It is considered the worst nuclear power plant accident in history, and it is the only one classified as a level 7 event on the International Nuclear Event Scale.
The disaster began during a systems test on 26 April 1986 at reactor number four of the Chernobyl plant, which is near the town of Pripyat. There was a sudden power output surge, and when an emergency shutdown was attempted, a more extreme spike in power output occurred, which led to a reactor vessel rupture and a series of explosions. This event exposed the graphite moderator of the reactor to air, causing it to ignite.[1] The resulting fire sent a plume of highly radioactive smoke fallout into the atmosphere and over an extensive geographical area, including Pripyat. The plume drifted over large parts of the western Soviet Union and Europe. From 1986 to 2000, 350,400 people were evacuated and resettled from the most severely contaminated areas of Belarus, Russia, and Ukraine.[2] According to official post-Soviet data,[3][4] about 60% of the fallout landed in Belarus.
The accident raised concerns about the safety of the Soviet nuclear power industry, as well as nuclear power in general, slowing its expansion for a number of years and forcing the Soviet government to become less secretive about its procedures.[5][notes 1]
Russia, Ukraine, and Belarus have been burdened with the continuing and substantial decontamination and health care costs of the Chernobyl accident. Thirty one deaths are directly attributed to the accident, all among the reactor staff and emergency workers. Estimates of the number of deaths potentially resulting from the accident vary enormously; the World Health Organization (WHO) suggest it could reach 4,000 while a Greenpeace report puts this figure at 200,000 or more. A UNSCEAR report places the total deaths from radiation at 64 as of 2008.

The attempted experiment

Even when not actively generating power, nuclear power reactors require cooling, typically provided by coolant flow, to remove decay heat.[7] Pressurized water reactors use water flow at high pressure to remove waste heat. After an emergency shutdown (scram), the core still generates a significant amount of residual heat, which is initially about seven percent of the total thermal output of the plant. If not removed by coolant systems, the heat could lead to core damage.[8][9] The reactor that exploded in Chernobyl consisted of about 1,600 individual fuel channels, and each operational channel required a flow of 28 metric tons (28,000 liters (7,400 USgal)) of water per hour.[6]:7 There had been concerns that in the event of a power grid failure, external power would not have been immediately available to run the plant's cooling water pumps. Chernobyl's reactors had three backup diesel generators. Each generator required 15 seconds to start up but took 60–75 seconds[6]:15 to attain full speed and reach the capacity of 5.5 MW required to run one main cooling water pump.[6]:30
This one-minute power gap was considered unacceptable, and it had been suggested that the mechanical energy (rotational momentum) of the steam turbine and residual steam pressure (with turbine valves closed) could be used to generate electricity to run the main cooling water pumps while the generator was reaching the correct RPM, frequency, and voltage. In theory, analyses indicated that this residual momentum and steam pressure had the potential to provide power for 45 seconds,[6]:16 which would bridge the power gap between the onset of the external power failure and the full availability of electric power from the emergency diesel generators. This capability still needed to be confirmed experimentally, and previous tests had ended unsuccessfully. An initial test carried out in 1982 showed that the excitation voltage of the turbine-generator was insufficient; it did not maintain the desired magnetic field after the turbine trip. The system was modified, and the test was repeated in 1984 but again proved unsuccessful. In 1985, the tests were attempted a third time but also yielded negative results. The test procedure was to be repeated again in 1986, and it was scheduled to take place during the maintenance shutdown of Reactor Four.[10]
The test focused on the switching sequences of the electrical supplies for the reactor. The test procedure was to begin with an automatic emergency shutdown (SCRAM). No detrimental effect on the safety of the reactor was anticipated, so the test program was not formally coordinated with either the chief designer of the reactor (NIKIET) or the scientific manager. Instead, it was approved only by the director of the plant (and even this approval was not consistent with established procedures). According to the test parameters, the thermal output of the reactor should have been no lower than 700 MW at the start of the experiment. If test conditions had been as planned, the procedure would almost certainly have been carried out safely; the eventual disaster resulted from attempts to boost the reactor output once the experiment had been started, which was inconsistent with approved procedure.[11]
The Chernobyl power plant had been in operation for two years without the capability to ride through the first 60–75 seconds of a total loss of electric power, and thus lacked an important safety feature. The station managers presumably wished to correct this at the first opportunity, which may explain why they continued the test even when serious problems arose, and why the requisite approval for the test had not been sought from the Soviet nuclear oversight regulator (even though there was a representative at the complex of 4 reactors).[notes 2]:18–20
The experimental procedure was intended to run as follows:
  1. The reactor was to be running at a low power level, between 700 MW and 800 MW.
  2. The steam turbine was to be run up to full speed.
  3. When these conditions were achieved, the steam supply was to be closed off.
  4. Generator performance was to be recorded to determine whether it could provide the bridging power for coolant pumps.
  5. After the "momentum" was used up at the normal operating RPM, frequency, and voltage the turbine/generator would be allowed to freewheel down.

    Conditions prior to the accident

    The conditions to run the test were established before the day shift of 25 April 1986. The day shift workers had been instructed in advance and were familiar with the established procedures. A special team of electrical engineers was present to test the new voltage regulating system.[12] As planned, a gradual reduction in the output of the power unit was begun at 01:06 on 25 April, and the power level had reached 50% of its nominal 3200 MW thermal level by the beginning of the day shift. At this point, another regional power station unexpectedly went off line, and the Kiev electrical grid controller requested that the further reduction of Chernobyl's output be postponed, as power was needed to satisfy the peak evening demand. The Chernobyl plant director agreed and postponed the test.
    At 23:04, the Kiev grid controller allowed the reactor shut-down to resume. This delay had some serious consequences: the day shift had long since departed, the evening shift was also preparing to leave, and the night shift would not take over until midnight, well into the job. According to plan, the test should have been finished during the day shift, and the night shift would only have had to maintain decay heat cooling systems in an otherwise shut down plant. The night shift had very limited time to prepare for and carry out the experiment. A further rapid reduction in the power level from 50% was actually executed during the shift change-over. Alexander Akimov was chief of the night shift, and Leonid Toptunov was the operator responsible for the reactor's operational regimen, including the movement of the control rods. Toptunov was a young engineer who had worked independently as a senior engineer for approximately three months.[6]:36–8
    The test plan called for the power output of reactor 4 to be gradually reduced to a thermal level of 700–1000 MW.[13] The level established in the test program (700 MW) was achieved at 00:05 on April 26; however, because of the natural production of the neutron absorber xenon-135 in the core, reactor power continued to decrease, even without further operator action. As the power reached approximately 500 MW, Toptunov mistakenly inserted the control rods too far, bringing the reactor to an unintended near-shutdown state. The exact circumstances are hard to know, because both Akimov and Toptunov died from radiation sickness.
    The reactor power dropped to 30 MW thermal (or less)—an almost completely shut down power level, which was approximately 5 percent of the minimum initial power level established as safe for the test.[11]:73 Control-room personnel consequently made the decision to restore the power and extracted the reactor control rods,[14] and several minutes elapsed between their extraction and the point that the power output began to increase and subsequently stabilize at 160–200 MW (thermal). This maneuver withdrew the majority of control rods to the rods' upper limits, but the low value of the operational reactivity margin restricted any further rise of reactor power. The rapid reduction in the power during the initial shutdown, and the subsequent operation at a level of less than 200 MW led to increased poisoning of the reactor core by the accumulation of xenon-135.[15] This made it necessary to extract additional control rods from the reactor core in order to counteract the poisoning.
    The operation of the reactor at the low power level with a small reactivity margin was accompanied by unstable core temperature and coolant flow, and possibly by instability of neutron flux.[16] Various alarms started going off at this point. The control room received repeated emergency signals regarding the levels in the steam/water separator drums, as well as of relief valves opened to relieve excess steam into a turbine condenser and of large excursions or variations in the flow rate of feed water, and also from the neutron power controller. In the period between 00:35 and 00:45, emergency alarm signals concerning thermal-hydraulic parameters were ignored, apparently to preserve the reactor power level. Emergency signals from the reactor emergency protection system (EPS-5) triggered a trip which turned off both turbine-generators.[17]
    After a while, a more or less stable state at a power level of 200 MW was achieved, and preparation for the experiment continued. As part of the test plan, extra water pumps were activated at 01:05 on 26 April, increasing the water flow. The increased coolant flow rate through the reactor produced an increase in the inlet coolant temperature of the reactor core, which now more closely approached the nucleate boiling temperature of water, reducing the safety margin. The flow exceeded the allowed limit at 01:19. At the same time, the extra water flow lowered the overall core temperature and reduced the existing steam voids in the core.[18] Since water also absorbs neutrons (and the higher density of liquid water makes it a better absorber than steam), turning on additional pumps decreased the reactor power further still. This prompted the operators to remove the manual control rods further to maintain power.[19]
    All these actions led to an extremely unstable reactor configuration. Nearly all of the control rods were removed, which would limit the value of the safety rods when initially inserted in a scram condition. Further, the reactor coolant had reduced boiling, but had limited margin to boiling, so any power excursion would produce boiling, reducing neutron absorption by the water. The reactor was in an unstable configuration that was clearly outside the safe operating envelope established by the designers.




Nema komentara:

Objavi komentar